Took a little time for the holidays plus an away vaca during the past month. Getting back to it.
While I still had a decent amount of depth to cut, I experimented a bit trying to improve finish. With the direction grinder is turning, and I'm pulling sled from headstock toward tail stock end, that would be "down grinding".
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I tried up grinding, by swapping the direction, and pulling from TS side toward HS side. Didn't change anything for me, and its more dangerous as I have to stop on a dime at HS end. So I swapped back to original of starting at HS end and pulling toward TS end.
In with swapping wheels, dressing etc I ended up with an increased vibration that I could fell, hear, and transfered to the work in a horrible finish. Another mis-adventure, either from the vibration or maybe when I swapped wheels, or both ? But one of two compound screws loosened and the compound moved by a degree, from 45 to 46 degrees. I caught it right after dressing a wheel and coming in to kiss off. . .
I finally got aggravated enough to start addressing known problems. I know how the washers/clamps sat on grinders arbor was a problem, plus wheel being unbalanced. First looking at the arbor. Main portion for wheel measures .499"-.500". The step that inner wheel clamp sits is .575", so a whole .0375" around circumference to contact the clamp. Making matters worse, there's a trench wide enough for clamp/washer to drop into at .490".
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First fix/patch, I sliced a thin piece of scotch tape, measuring .001" thick, and wrapped in that trench so clamp will sit more true. This worked and helped with vibration as clamp itself is spinning centered.
Next I cleaned up mating surface of clamps to sit on that interior step more squarely:
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Note*: You can't have a grinding wheel itself tight or snug on an arbor. There's always a few thou's atleast. This allows thermal expansion or arbor and wheel. Otherwise wheel could fracture or blow apart if no room for thermal growth.
Now knowing that, I'm still trying to reduce a balancing problem and reduce vibration. And looking at how you typically get 6" wheels, there's several removable adapters inside to fit 1/2" up to 1" arbors:
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Even though I have been dressing wheels, I think I had gotten off centered, and though dressed, more weight was still to one side. To fix, I got a brand new 60 grit green silicon. I just slightly snugged with clamps and nut on arbor. I then used a dial indicator with a garbage flat tip and indicated with wheel in as close as possible before tightening wheel. Tightening pulled me off center a few thou, but I was close. Then dressed wheel
The result of these fixes has the grinder running the absolute smoothest since I began, and naturally it shows on the finish of the work. Grinder powered off, I can rotate and stop the wheel anywhere in 360 degrees, and stays put, no more rolling the heavy side to 6 oclock. So I know I nailed the balance pretty good.
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